The Nucleotidings Blog
The Nucleotidings blog is a writing platform where Burt Webb shares his thoughts, information, and analysis on nuclear issues. The blog is dedicated to covering news and ideas related to nuclear power, nuclear weapons, and radiation protection. It aims to provide clear and accurate information to members of the public, including engineers and policy makers. Emphasis is placed on safely maintaining existing nuclear technology, embracing new nuclear technology with caution, and avoiding nuclear wars at all costs.

Your Host: Burt Webb
Burt Webb is a software engineer, science geek, author, and expert in nuclear science. Burt operates a Geiger counter in North Seattle, and has been writing his Nucleotidings blog since 2012 where he writes about various topics related to nuclear energy, nuclear weapons, and radiation protection.

Burt Webb has published several technical books and novels. He works as a software consultant.

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Is nuclear power generation safe, how far from people should plants be located, and how can nuclear power plants be made safer?

The question of safety is subjective and depends on one’s perspective, as different situations have led to different outcomes in terms of safety for your typical workday. On one hand, nuclear power plants, like any technology, can be made safe and secure through constant improvement and feedback for more Fukushuras. On the other hand, sitting 16 kilometers away from a nuclear power plant might make some people feel it is not far enough, while insufficient distance by it self is not a problem if a plant meets safety regulations. Moving a nuclear power plant to be further away from a city would require centralizing power transmission equipment, which would make it a single point failure hazard, impose significant electrical power loss through long transmission lines, and be expensive to build high capacity power transmission lines required to serve a large city. Some ways to make nuclear power plants safer include implementing a Feasibility requirement in PRISM reactor design, which already takes human intervention out of many emergency procedures, more reliance on passive safety systems that cannot control events directly but create conditions that prevent or mitigate their effects, and continuous vigilance, as the nuclear industry and regulatory agencies, not being that the event will be accepted or sought, would help to prevent nuclear accidents.

What do you mean by “Fukushuras”?

“Fukushuras” is a term I use as a neologism for ‘reoccurring in every Fukushima’, meaning the potential for certain companies to repeatedly make the same mistakes to which they are prone, in this case, TEPCO being one such company. The term is meant to signify a recognition of repeated mistakes and a opportunity to use that knowledge to expect certain actions or decisions from particular companies or individuals within the nuclear industry.

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  • U.S. Nuclear Reactors 8 – Peach Bottom, Pennsylvania

              The Peach Bottom Atomic Power Station is fifty miles southeast of Harrisburg, Pennsylvania and draws cooling water from the Susquehanna River.  Unit One was an experimental reactor that only operated for eight years and was shut down in 1974. Unit Two and Unit Three are General Electric boiling water reactors rated at one thousand two hundred megawatts each. The Philadelphia Electric Company built and put the two units into operating in 1973 and 1974.  Unit Two was licensed until 2003 and had the license renewed in 2003 for an additional twenty years until 2033. Unit Three was licensed until 2004 and had the license renewed in 2004 for an additional twenty years until 2034. The Philadelphia Electric Company eventually became Exelon.

              The population in the plume exposure pathway zone with a radius of ten miles around the plant contains about forty seven thousand people. The ingestion pathway zone with a radius of fifty miles around the plant contains about five and a half million people. The estimated risk of an earthquake that could damage the plant is moderate.

               In 1987, the NRC ordered the shutdown of Unit Two and Unit Three because of “operator misconduct, corporate malfeasance and blatant disregard for the health and safety of the area.” The NRC reported that security guards were overworked and that one guard had been found sleeping on duty. Thirty six thousand gallons of mildly radioactive water were leaked into the Susquehanna river. The operators claimed to have mislaid data on radioactive waste classification which resulted in the shipment of radioactive waste assigned to the wrong category. There was a major fire in March 0f 1987 in Unit Three. In May of 2000, a valve failed which caused a leak of contaminated coolant outside of primary containment. The valve was not replaced and another leak occurred in August of 2000 resulting in a shutdown of the reactor.  In 2007, a former employee at Peach Bottom videotaped guards sleeping while on duty. There were also reports of workers slowed down the testing of reactor control rods in order to evade NRC regulations which would have required a shut down. It was found later that the NRC knew about the deception but failed to deal with it in a proper and timely manner.

              In the case of Peach Bottom, we have major leaks of radioactive water into the environment, breakdown of equipment that was not repaired after it had been found, staff sleeping on duty, dishonesty on the part of the operator to avoid shutdowns, misclassification of nuclear waste that may have posed a public health problem and incompetence on the part of the NRC in holding the operators to account for blatant disregard of regulations.

  • U.S. Nuclear Reactors 8 – Peach Bottom, Pennsylvania

              The Peach Bottom Atomic Power Station is fifty miles southeast of Harrisburg, Pennsylvania and draws cooling water from the Susquehanna River.  Unit One was an experimental reactor that only operated for eight years and was shut down in 1974. Unit Two and Unit Three are General Electric boiling water reactors rated at one thousand two hundred megawatts each. The Philadelphia Electric Company built and put the two units into operating in 1973 and 1974.  Unit Two was licensed until 2003 and had the license renewed in 2003 for an additional twenty years until 2033. Unit Three was licensed until 2004 and had the license renewed in 2004 for an additional twenty years until 2034. The Philadelphia Electric Company eventually became Exelon.

              The population in the plume exposure pathway zone with a radius of ten miles around the plant contains about forty seven thousand people. The ingestion pathway zone with a radius of fifty miles around the plant contains about five and a half million people. The estimated risk of an earthquake that could damage the plant is moderate.

               In 1987, the NRC ordered the shutdown of Unit Two and Unit Three because of “operator misconduct, corporate malfeasance and blatant disregard for the health and safety of the area.” The NRC reported that security guards were overworked and that one guard had been found sleeping on duty. Thirty six thousand gallons of mildly radioactive water were leaked into the Susquehanna river. The operators claimed to have mislaid data on radioactive waste classification which resulted in the shipment of radioactive waste assigned to the wrong category. There was a major fire in March 0f 1987 in Unit Three. In May of 2000, a valve failed which caused a leak of contaminated coolant outside of primary containment. The valve was not replaced and another leak occurred in August of 2000 resulting in a shutdown of the reactor.  In 2007, a former employee at Peach Bottom videotaped guards sleeping while on duty. There were also reports of workers slowed down the testing of reactor control rods in order to evade NRC regulations which would have required a shut down. It was found later that the NRC knew about the deception but failed to deal with it in a proper and timely manner.

              In the case of Peach Bottom, we have major leaks of radioactive water into the environment, breakdown of equipment that was not repaired after it had been found, staff sleeping on duty, dishonesty on the part of the operator to avoid shutdowns, misclassification of nuclear waste that may have posed a public health problem and incompetence on the part of the NRC in holding the operators to account for blatant disregard of regulations.

  • U.S. Nuclear Reactor 7 – Vermont Yankee, Vermont

              The Vermont Yankee Nuclear Power Plant is located in Vernon, Vermont. It has  a six hundred and twenty megawatt General Electric boiling water reactor that draws cooling water from the reservoir pool of the Vernon Hydroelectric Dam on the Connecticut River. It was put into operation in 1972 and was licensed for forty years until 2012. Entergy Nuclear currently owns and operates the power plant.

              Vermont Yankee was built by a group of big utility companies. In 2001, the utilities tried to sell Vermont Yankee to AmerGen for sixty one million dollars but the Vermont’s Public Service Board said that an auction was necessary if they wanted to sell the power plant. In 2002, the utilities sold the plant to Entergy Nuclear for one hundred and eighty million dollars. Entergy and Vermont agreed that they would abide by the decision of Vermont’s Public Service Board on the question of whether Vermont Yankee should continue to operate after their original license ran out in 2012. In 2006, the Vermont legislature passed a law that required the Public Service Board to obtain the approval of the legislature before considering the extension of the plant’s license past the expiration of the original license.

              The population in the plume exposure pathway zone with a radius of 10 miles around the plant is about thirty five thousand people. The population in the ingestion pathway zone with a radius of fifty miles around the plant is about one million five hundred and forty thousand people. The risk of a seismic event that could threaten the plant is rated as very low.

               In 2007, part of the west cooling tower collapsed due to corrosion in steel bolts and rotting lumber. Non-radioactive water was spilled into the environment. The NRC review of the accident said that they considered this to be an industrial accident that did not pose a threat to the reactor. A Vermont study concluded that Vermont Yankee was being operated in a safe manner and did not pose a public threat.

              In May 2009, the special oversight committee appointed by the Vermont legislature heard testimony from plant operators that there was no radioactive contamination of ground water from leaking underground pipes. However, in October of 2009, it was confirmed that there really was radioactive contamination leaking from underground pipes at the plant. Entergy was accused of making misleading statements and was told that they would be liable for some legal expenses relating to the leak.

               By 2010, the level of radioactive tritium in ground water around the plant had risen above the federal limit for safe levels and ultimately reached one hundred times the limit for safe drinking water. Eventually, the leaks were traced to a pair of steam pipes in a pipe tunnel and the leaking pipes were repaired. Later in 2010, a water leak caused by a faulty weld caused a short shut down of the plant for repairs.

            In 2011, more tritium was detected in ground water but the source has not yet been identified.

            In early 2010, the Vermont legislature voted to instruct the Vermont Public Service Board to reject the request of a license extension of Vermont Yankee beyond 2012. The NRC ultimately issued the license extension in 2011. Entergy sued the state of Vermont to overturn the ban of a license extension passed by the state legislature. In 2012, the U.S District Court ruled that Vermont did not have the authority to deny the new license and that such matters were the exclusive province of the NRC.

             Vermont Yankee had design problems that led to serious leaks of tritium and the owners lied about the leaks. The state of Vermont tried to prevent the plant from continuing to operate but the U.S. District Court said that they did not have the right to shut down a nuclear power plant in their state that they considered to be a danger to their citizens.

  • U.S. Nuclear Reactors 6 -Braidwood, Illinois

                  The Braidwood Nuclear Generating Station (BNGS) is located in northeastern Illinois near Joliet and draws it water from the Kankakee River. It was originally built by Commonwealth Edison and ultimately transferred to Exelon Corporation, the parent company of Commonwealth Edison.  The Station contains two Westinghouse pressurized water reactors. The Unit 1 reactor was put into operation in 1987 and is licensed by the NRC to operate until 2026. The Unit 2 reactor was put into operation in 1988 and is licensed by the NRC to operate until 2027. The total generating capacity of the BNGS is two thousand two hundred forty two megawatts. It supplies power to Chicago and other consumers in northeastern Illinois.

                 The population in the NRC plume exposure pathway zone with a ten mile radius is about thirty four thousand people.  The population in the NRC plume ingestion pathway zone with a fifty mile radius is about five million people.   The risk of a seismic event that could threaten the BNGS is rated as very low by the NRC.

                   In March of 2011, it was discovered that an alarm was not functioning because of faulty wiring and that there was a problem with back-up pipes. Over a period of years, six million gallons of water containing tritium were leaked into the water table under the BNGS without any notification of the people who live in that area. Both Exelon, owner of the BNGS, and the NRC have claimed that there was no public health threat from the leaking tritium but people in the area are claiming that the leaking tritium has cause severe health problems. With the revelation of the leak, the value of real estate around the plant has dropped and some people are unable to sell their property.

                  The NRC has stated that Exelon has repaired the problems with the alarm system that should have warned that tritium was leaking. Exelon has also replaced flawed back-up pipe. In May of 2011, the NRC held an unprecedented public meeting to allay public fears about the leaking tritium.

                 Power plants that use water for cooling such as nuclear, coal and oil are designed to run at lower power output during the summer months because of higher temperatures of cooling water. In July of 2012, the BNGS had to ask special permission from the NRC to continue operating after the water temperature in the cooling pond rose above 102 degrees. The plant is supposed to shut down completely in six hours if the water temperature of the cooling pond rises above 100 degrees, an event which had been extremely rare until recently. It would have been disastrous to have to shut down a two thousand megawatt plant right in the middle of the worst heat wave in thirty years.

                At the BNGS, they had an improperly installed alarm and faulty piping resulting in a huge leak of water contaminated with tritium. This caused great fear and concern on the part of the people living around the plant. The rising temperatures of global warming will continue to interfere with the proper operation of the plant and it may have to be shut down completely if the temperature increase continues, a likely eventuality.

    Picture from Northwestern University.

  • Nuclear Debate 11 – 10 Signs That the Nuclear Industry is Ailing

                 The nuclear industry is in serious trouble these days. It if was not so huge and tightly involved with national governments, it would have collapsed long ago.  I got this list of problems for the nuclear industry off the Nuclear-News website and have added a few comments of my own.

    1. Widespread assumption that another major accident is inevitable.  Regulatory agencies are not doing their job in many cases because they have been “captured” by the industry. Nuclear corporations are cutting corners, ignoring regulations, making unauthorized design changes and not insuring that staffs are sufficiently trained.
    2. Many of the world’s commercial nuclear power reactors are nearing the end of their design lifespan and require repairs that are too expensive to continue to function.
    3. Very few nuclear reactors have been built in the past few decades to take advantage of design improvement and lessons learned.
    4. Competition for a shrinking international market in reactors has been increasing as nuclear companies that cannot sell new reactors in their home countries are trying to survive and new designs are frantically hyped.
    5. Climate change threatens nuclear reactors with rising ocean temperatures, dropping water levels in rivers, and mega storms that can damage or floor reactors.
    6. Nuclear weapon inventories are being reduced by treaty. Even an exchange of a few hundred warheads could bring a nuclear winter that would destroy our civilization. Global conflicts are now asymmetrical with major countries fighting terrorist groups in the third world. Nuclear deterrence is no longer a reasonable way to deal with international tensions if it ever was.
    7. The world consumption of electricity has been dropping as conservation measures are being implemented and industries are being idled by world financial problems.
    8. The cost of renewable energy is dropping as the cost of nuclear power is rising. It is only a matter of time before nuclear power is simply no longer competitive in the marketplace.
    9. The entire nuclear fuel cycle from mining to refining to transporting to burning to storing waste is vulnerable to accidents or terrorist attacks. Other forms of energy are just not as dangerous as nuclear power for this standpoint.
    10. Public opinion has been turning against nuclear power recently, especially since the nuclear disaster at Fukushima in Japan.

     

    None of these problems is going to go away and many of them are only going to get worse with the passage of time. All of these problems add up to make the further use of nuclear energy for electrical power generation less and less attractive. Another major accident or a terrorist use of nuclear materials could be the fatal blow that brings down the house of cards that is the nuclear industry.

  • U.S. Reactors 5 – Palisades, Michigan

                The Palisades Nuclear Plant is located on Lake Michigan near South Haven, Michigan. The reactor is a Combustion Engineering pressurized water reactor that was put into operation at the end of 1971. It can generate up to seven hundred and fifty megawatts of electricity. It was owned by CMS Energy Corporation and operated by the Nuclear Management Company prior to April of 2007 at which time it was purchased by Entergy. The reactor was originally licensed to 2011. A twenty year extension was applied for in 2005 and granted in 2007.

                The NRC plume exposure pathway zone with a radius of ten miles contains about thirty thousand people. The NRC ingesting pathway zone with a radius of fifty miles contains about one million three hundred thousand people. The risk of an earthquake that could damage the reactor is extremely low according to the NRC.

                There are twenty one dry storage casks on the grounds that contain a total of six hundred and thirty tons of spent fuel. The casks were intended to be temporary storage until the Yucca Mountain Repository was opened. However, the Yucca Mountain Repository project was cancelled and the spent fuel will remain at the site until an alternative permanent storage facility is developed.

                 The Palisades Nuclear Plant has been rated as one of the three most unsafe reactors in the whole United States by the NRC. In the past two years, it has had dozens of leaks and been shut down seven times. However, the NRC announced at the end of 2012 that the reactor is no longer unsafe because they have increased in the number of inspections at the plant. The most recent shutdown took place in the middle of February, 2013. After a week was spent tracking down a leak in the cooling system, the reactor was restarted.

                  Local critics want the plant shut down permanently. They say that it is one of the oldest plants in the country and is disintegrating. They complain that the NRC has been focusing on staff and safety culture and that that is not enough. I would have to agree. It sounds like the plant and it’s equipment are falling apart. It is all very good and well for the NRC to make sure that the staff is following proper safety protocols but if the plant is just too old to maintain, all the inspections and safety protocols in the world will not prevent another problem with the physical plant.

                 The problems at this power plant appear to involve aging components and bad safety practices. The second is easier to correct than the first. And, the NRC would seem to be a little too optimistic in stating that the plant is now safe. Even with the best staff in the world, the NRC should not have granted a twenty year extension of the license. At best, there will be additional leaks, shutdowns and expensive repairs. The plant may fail completely and have to be shut down long before the twenty year extension has run out. And, of course, the worst case would be for a major accident to occur.

  • U.S. Nuclear Reactors 4 – Oyster Creek, New Jersey

                 The Oyster Creek Nuclear Generation Station is located in Lacey Township of New Jersey. It is a General Electric Type 2 boiling water reactor that generates  six hundred forty five megawatts. It gets cooling water from Barnegat Bay, an estuary that empties into the Atlantic Ocean. It is the oldest operating reactor in the United States.             Around 1990, it was discovered that the drywell lining of the reactor containment vessel was corroding. The exterior of the drywell shell was cleaned of corrosion and a new coating of epoxy was applied. There has been no further report of corrosion problems.

                  The NRC plume exposure pathway zone with a ten mile radius contains about one hundred thirty thousand people. The NRC ingesting pathway zone with a radius of fifty miles contains about four and a half million people. The biggest concern about the safety of the plant has to do with the possibility of flooding.

                 The Oyster Creek reactor was put into operation in 1969 with a forty year license. Jersey Power and Light owned by General Public Utilities merged with Free Energy in 2001 and sold the plant to AmerGen for ten million dollars in a transaction that was challenged by the NRC who feared that AmerGen was not competent enough to successfully and safely run the reactor. Exelon purchased AmerGen in 2003 and currently owns and operates the plant.

                  In 2005, Exelon applied for a twenty year extension of the operating license which was eventually granted after contentious hearing. Both Exelon and the NRC were criticized because they used environmental studies that were thirty years old in considering environmental impacts of the extended license. During the relicensing hearing, anti-nuclear groups complained that the metal in the core of the reactor had not been tested for brittleness that often results from long exposure to super hot water and intense radiation. The license was granted in 2009.

                 Shortly after the new license was granted a tritium leak was found in two buried pipes that had not been insulated correctly in 1991 when the pipes had been worked on. Then a second tritium leak was discovered in August of 2009. For the last twenty years tritium has been contaminating the ground water and has flowed into Barnegat Bay. The tainted water has spread to an aquifer in the area and will reach public wells within ten years. They are working on dealing with the problem.

                In late 2010, Exelon stated that it would be closing and decommissioning the Oyster Creek reactor in 2019, ten years before the expiration of its new license. If they continued to operate past 2019, they would have to build expensive new cooling towers. There are also the cost of repairs and remediation due to the contaminated water to consider.

               When Hurricane Sandy hit last year, the rising water threatened the reactor and it was shut down. There is speculation that if the water had risen a few more feet in the estuary, the reactor site could have been flooded.

               The Oyster Creek situation includes lack of regulator vigor on the part of the NRC, siting issues, poor original design, and incompetent contractors causing damage that leads to leaks of radioactive water.

  • U.S. Nuclear Reactors 3 – Crystal River, Florida

                  The Crystal River Nuclear Power Plant is located in the Crystal River Energy Complex eight miles north of Crystal River, Florida on the Gulf of Mexico. The reactor is a pressurized water reactor capable of generating eight hundred and sixty megawatts. It shares the complex with four fossil fuel power plants.

                The Crystal River plant was constructed by Florida Progress Corporation and went into operation in 1977. It was operated by a subsidiary, Florida Power Corporation. In 2000, it was purchased by Carolina Power & Light and a new company called Progress Energy was formed. In 2012, it was bought by Duke Energy which now operates it. Duke controls around ninety percent and the other ten percent is owned by nine municipal utilities. Its license was scheduled to run out in 2016.

                 In September of 2066, a 5.8 magnitude earthquake occurred about three hundred miles to the southwest of the plant but no damage to the plant occurred. The odds of an earthquake powerful enough to damage the reactor are estimated to be very low. The NRC plume exposure pathway zone with a radius of ten miles contains more than twenty thousand people. The NRC ingestion pathway zone with a fifty miles radius contains over one million people.

                  In September of 2009, the plant was shut down for refueling and to increase the power output. A hole was cut into the containment vessel to replace the steam generators but it turned out that the concreted of the containment vessel had been overstressed by the workers cutting the hole and the concrete was damaged. That section was repaired but the repairs caused problems in other areas of the concrete shell. The plant had been scheduled to restart in April of 2011 but in June of that year, the restart was put off until 2014.

                 The initial estimate of the cost of repairs was between nine hundred million dollars and one billion three hundred million dollars. In October of 2012, that estimate was revised by an independent review to between one billion five hundred million and three billion four hundred million dollars. In February of 2013, Duke Energy announced that the Crystal River Nuclear Power Plant will never be restarted. They are going to shut it down permanently. It may take up to sixty years for the site to be dismantled and decontaminated.

                 Duke will provide eight hundred and fifty million dollars in  settlements to the customers who had to purchase electricity at a higher cost. Duke claims that the Nuclear Electric Insurance company shortchanged Duke customers for the more expensive electricity. Duke will also try to recover the one billion six hundred and fifty million dollars that it paid for the purchase of the plant from its customers.

                  Here we have a case of an old nuclear power plant that may have had a poorly constructed containment vessel in the first place and had the containment vessel damaged by incompetent contractors. It would seem a poor decision on the part of Duke Energy to purchase an old reactor near the end of its license that was in the middle of expensive and problematic repairs. There are also issues with the integrity and/or competence of the company insuring in the customers of a nuclear power station. And finally, I question whether or not a company with the poor judgment of Duke Energy will actually be able to survive long enough to oversee the sixty year process of decommissioning the power plant.

    Picture from Nuke plant:

     

  • U.S. Nuclear Reactors 2 – San Onofre, California

                  The San Onofre Nuclear Generating Station (SONGS) is located on the Pacific Coast of California near San Diego. SONGS is owned and operated by Southern California Edison and San Diego Gas & Electric Company and has supplied as much as 20% of the power to areas of Southern California.

                   Unit 1 is a first generation Westinghouse pressurized water reactor that was constructed in 1967 by Bechtel Corporation, operated for twenty five years and then was permanently shut down in 1992. The reactor has been dismantled and the building is used to store spent nuclear fuel. Units 2 and 3 are Combustion Engineering pressurized water reactors that each generate about one megawatt of electricity when operating at full capacity. There are four thousand tons of waste stored at the plant.

                  SONGS was designed and built to be able to survive a seven magnitude earthquake under the plant and there is a twenty five foot tsunami wall to protect against tidal waves caused by the active fault five miles offshore. The plant uses ocean water for cooling the reactors but may have to build huge cooling towers if new regulations restrict the direct use of sea water for reactor cooling.

                  There are about ten thousand people in the NRC emergency plume exposure pathway zone within a ten mile radius of the plant. They might be exposed to airborne radioactive particles in the event of a leak at SONGS. About eight and one half million people live in the ingestion pathway zone within a fifty mile radius of the plant. The main risk for them is possible ingestion of radioactive particles from food or water within the zone.

                   SONGS has been plagued by problems since it was built. There have been major and costly mistakes made in the installation of equipment. The NRC has issued multiple citations for such things as failure of emergency generators, improperly wired batteries and falsification of fire safety data. A recent NRC reports stated that there had not been sustained improvements in the performance of the staff at the plant.

                   Both Unit 1 and Unit 2 reactors have been shut down for the past year due to the discovery of unexpected corrosion in pipes resulting in leaks in the steam generators. The operators promised not to restart the reactors until the cause of the problem had been found and corrected.  Critics claim that there were many changes in design and equipment that were not properly reviewed by the NRC.

                    By the middle of 2012, the cost of the shutdown had risen to one hundred and sixty five million dollars, one hundred and seventeen of which had to be spent to buy power from other sources to replace the lost of power from the plant. Reactor 3 may not be restarted because of extensive and expensive repairs that would be required. By late 2012, the cost of the shutdown had reached three hundred million dollars and talks with the NRC over restarting Reactor 2 had been postponed.

                    Considering what the shutdown has already has already cost and what additional cost might lie ahead for repairing Reactor 2, it may turn out that San Onofre may never be restarted. Hundreds of millions of extra dollars will have to be spent to decommission Reactor 3 at the least and more if Reactor 2 is not restarted. This appears to be a case of incompetence and refusal to follow regulations on the part of the operators resulting in the closing of a nuclear power plant.

    Picture from awnisALAN:

  • U.S. Nuclear Reactors 1 – Kewaunee, Wisconsin

             I have discussed the United States nuclear reactor fleet in previous posts and have also dealt with problems with specific U.S. reactors. This post is going to be the first of a series that highlights each of the U.S. reactors in turn with emphasis on problems.

             The Kewaunee Power Station has one Westinghouse pressurized water reactor and is located on a nine hundred acre site in Carlton, Wisconsin, just southeast of Green Bay. It was constructed in 1972 and was originally owned by Wisconsin Public Service and Alliant Energy. Nuclear Management Company operated the plant from 2000 to 2005. Dominion Resources currently owns and operates the plant. In 2008, Dominion applied to the NRC to extend the license to operate the plant for an extra twenty years until 2033 and the license request was granted.

              The NRC regulations define two risk zones around nuclear power plants. There is a ten mile in diameter zone around a reactor where the main risk is that a plume of radioactivity leaking from the plant would threaten people with the possibility of the inhalation of airborne radioactive particles. There are about ten thousand people in that zone at Kewaunee. The second zone is a fifty mile radius and contains the risk of ingestion of radioactive particles from eating contaminated food and/or drinking contaminated water. The second zone around Kewaunee contains about over three quarters of a million people. The Kewaunee plant has had coolant leaks but a good safety record overall. There is minimal risk of an earthquake in the area of the plant.

               At the end of 2012, Dominion Resources announced that they would shut down the plant and decommission it starting in 2013 although they were licensed for another twenty years. Dominion Resources had planned to add additional reactors to power stations that it owned in the Midwest to take advantage of the existing infrastructure. However, falling natural gas prices and the resultant dropping prices of electricity in the Midwest made their plans impractical from a strictly economic point of view.

              Two hundred eighty million dollars will be spent shutting down and decommissioning the Kewaunee reactor. This is sixty million dollars more than it cost Dominion Resources to purchase the plant in 2005. The site is supposed to be returned to what is called a “greenfield condition” within sixty years. I wonder what the odds are

              Many different options for the generation of electricity are being explored and the cost of some of them other than nuclear power and fossil fuels such as wind, solar, tidal, geothermal, and biofuels will become more competitive as time passes. Nuclear power stations have huge startup costs. The price of uranium is unstable. The problem of waste has still not been solved. There are many possible reasons to shut down nuclear plants but this particular plant is being closed because it just can’t compete on the open energy market